I have been using the ASC-1 controller for about 5 months now. Really love how it works! However I'm having a problem that did not occur with my G-Box controller. I'm almost always off about 8-10 counts to the West and have to move the dish 8-10 counts to land on the satellite. I have tried putting the capacitor (as mentioned on the Titanium web site) across the M1 & M2 wires at the actuator. Everything else seems good and tight. Any suggestions to try would be appreciated!
From the Titanium web site:
Connect a .01 µF, 50 volt (minimum rated) capacitor between the M1 and M2 wires at the actuator motor. The capacitor minimizes the motor RF noise from interfering with the sensor and servo control circuits.
From the Titanium web site:
Connect a .01 µF, 50 volt (minimum rated) capacitor between the M1 and M2 wires at the actuator motor. The capacitor minimizes the motor RF noise from interfering with the sensor and servo control circuits.